 |
VERTICAL
SHAFT BRICK KLIN TECHNOLOGY |
| Energy
efficient |
Environmentally
sound |
Economically
viable |
|
VSBK – 11, Hemant
Prajapati, Guna
|
 |
VSBK
12 is located on the Guna – Ashoknagar
highway approximately 18 kms from Guna on
the banks of Sindh river. A perspective view
of the kiln can also be had, traveling on
the Guna – Bina broad gauge railway line.
Layout of the kiln started on 10th.
December, 2001 and construction including
ramp was over by 5th. of January,
2002 in a record time of 26 days.
|
Previously
most of the construction work used to be completed
within a time frame of 45 days. However in VSBK –
12, faster construction was possible mainly due to:
- Timely
available of construction materials
- Higher
engagement of work force i.e. masons and
labours
- Dedication
and ownership responsibility in work of
workers
- Enthusiasm
and keenness of entrepreneur in the work being
carried out
- Able
supervision
Guna
kiln has been constructed at a 12 batch height due
to excellent quality of green bricks with 2 shafts
of nominal size 1m x 2m. In and around Guna, raw
material (soil) is processed by filtration technique
akin to ceramic processing, locally coined as GHOL
process. This is necessary to separate the morum
particles contained in the soil.
| The
process also ensures adequate plasticity of
the soil, proper ageing and uniform mixing
with added internal fuel and anti-shrinkage
materials. Although the method observed was
quite crude from the technological aspect
but was found to be extremely effective to
produce good quality bricks from inferior
quality soil. |
 |
Soil
for brick making is presently excavated from site
only. Due to highly undulating nature of the
topography, on an average 8 to 10 ft of soil can be
taken out for brick making. Enough soil is available
to last for a couple of years. Entrepreneur has also
thought of soil transportation to site in future.
The excavated soil is transported by donkeys to a
rectangular vat. Water is fed into the vat and the
soil-water mixture is agitated by a blunger. After
the soil is deflocculated and mixed intimately with
the water the resultant slurry is passed through a
2mm sieve. Residues in the form of morum, stone
particles are rejected. The slurry is
gravitationally transported through channels to
storage tanks of 10ft x 5ft dimension and depth of
3ft. After allowing a settling time of 24 hours the
water is decanted off by pump and manually also.
Wheat straw is added to this slurry about 2 – 4%
by weight and left to age for 4 days. During this
time besides ageing, extra moisture in the filtrated
soil evaporates, making it amenable for shaping by
jand moulding. After 4 days, internal fuel in the
form of cinder ash is mixed about 6 – 10% by
weight alongwith filler anti-shrinkage stone dust in
the quantity of 8 – 12% by weight. Addition of
stone dust helps in arresting the high shrinkage,
besides increasing the fired density and physico-mechanical
properties due to greater specific gravity compared
to soil. After the required external material
addition, the soil is mixed in the tank manually and
left to age for another 2 days. The entire process
is over by around 7 days whence the mixture is ready
for shaping into green bricks.
|
 |
| Soil
excavated from site or
transported |
|
|
|
 |
|
|
 |
| Mix
with water and agitated in
vat by blunger |
|
|
|
 |
|
|
 |
| Filtration
to separate > 2mm
particles |
|
|
|
 |
|
|
 |
|
 |
 |
|
Initially
the green bricks were being demoulded from moulds by
using fine coal dust. This not only increased the
cost, but also produced inferior surface colour
bricks. Entrepreneur was convinced to change the
demoulding material from coal dust to parting sand.
This not only drastically changed the colour of the
fired bricks but also gave a better surface finish
when fired in VSBK. The shapes of the frog in his
bricks were changed from tetragonal to elliptical in
shape along with the lettering PRAJA from Hindi to
English. Depth of the frog was increased by 2mm.
This will entail savings on soil thus increasing
profitability. Change in frog lettering although has
technological importance but provides a meaningful
social implication. It not only helps in
distinguishing his bricks from the nearby clamps but
also enhances his image among the generally
illiterate – semi illiterate belt with the English
monogram. Size of mould was also changed to increase
the size of the fired bricks. Previously his burnt
brick size was 8.75 in. x 4 in. x 2.25 in. which was
increased to 9 in. x 4.25 in. x 2.75 in. This size
is more acceptable in local conditions and also
stands out when compared to the local bricks being
produced.
 |
Although
construction was completed on 5th.
January, 2002, firing in first shaft
commenced on 10th. February,
2002. This delay of more than a month was
due to non-availability of trolley and screw
jack. Kiln equipments were supplied by Mr.
Narayan Das Prajapati and the inadvertent
delay was caused from his end only. During
this time entrepreneur was appraised of the
pros and cons of equipment supply by an in
experienced fabricator. |
Upon
inspection of the equipments, they were found to be
of improper quality and specifications.
To reduce the cost materials used were not of
required grade along with poor welding quality.
Entrepreneur was shown the problems and appraised of
the future problems on working with these materials.
Shaft I was initialized on 10th.
February, 2002. Initially the shaft was loaded in
double chulha pattern containing 80 + 64 + 80 + 64
total of 288 bricks along with 20 kg of external
fuel. Firing was started from the bottom. New
pattern of loading during firing initialization has
been followed from this season in all the newly and
also old kilns. This type of loading increases the
airflow thus helping in faster travel of fire. This
results is faster stabilization. After initial start
with 12 batches in double chulha pattern the old
Datia pattern was reverted to. This increased the
quantity of bricks loaded from 288 to 346. Coal
quantity after the first 24 hours of firing was
gradually reduced to 12 kg per batch which amounts
to 3.5 tonnes per lakh. After about 10 days of
stabilization coal quantity was further reduced to 9
kg per batch amounting to 2.5 tonnes per lakh. At
present external fuel consumption is around 1 tonnes
per lakh. Previously in clamp coal consumption was
around 2.5 tonnes per lakh. Thus VSBK firing has a
saving of around 60% of external fuel compared to
clamps. In VSBK firing on shaft I breakage is on an
average 6 bricks per batch equivalent to 1 % which
is worth mentioning compared to 4% breakage in
clamps. Good quality of green bricks of high green
strength reduces the breakage. Shaft II was fired on
4th. March, 2002 and was also stabilized
after 2 days. Breakage quantity and fuel consumption
is also similar to shaft I.
|
|
.....Go
Top
|
ENERGY
EFFICIENCY AND RENEWABLE ENERGY RESOURCES PROJECT
Sponsored
by : SWISS
AGENCY FOR DEVELOPMENT AND CO-OPERATION
|
|